MINIMASI WASTE DENGAN PENDEKATAN LEAN MANUFACTURING PADA PROSES PREPARATION – ASSEMBLY AREA P1C2A MODEL SEPATU BASEBALL BLACK DI PT. PANARUB DWIKARYA

NUR SITI SARA 15660020, NIM. 15660020 (2021) MINIMASI WASTE DENGAN PENDEKATAN LEAN MANUFACTURING PADA PROSES PREPARATION – ASSEMBLY AREA P1C2A MODEL SEPATU BASEBALL BLACK DI PT. PANARUB DWIKARYA. Skripsi thesis, FAKULTAS SAINS DAN TEKNOLOGI.

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Abstract

The Lean Manufacturing approach is a continuous improvement effort in the production process to identify the types and factors of waste occurrence by minimizing waste so that the value stream is smooth so that production time is more efficient. PT. Panarub Dwikarya is a company engaged in the fabrication of sports shoes such as Specs, Mizuno and Adidas. The quality, quantity and speed of production units play an important role in order to fulfill consumer demand. Lead time, defects, motion and transportation constraints are mostly carried out in the production process. This waste minimization is expected to increase the efficiency of production time so that the products produced can be on time with the right amount. From the results of the study, it was found that the lead time was reduced from 1999.31 seconds to 1847.22 seconds or reduced by 152.09 seconds (about 7.6%), as well as the transportation time from 360.52 seconds to 281.32 or reduced to 79,2 seconds (about 21.96%), as well as a reduction in the transportation distance from 2441 cm to 658 cm or a decrease of 1783 cm (about 73.04%). This is due to a reduction in non-value added activities, re-layout of the work area with Blocplan software, re-layout of work stations, and the addition of work operators.

Item Type: Thesis (Skripsi)
Additional Information: Tutik Farihah, M.Sc.
Uncontrolled Keywords: Lean Manufacturing, Seven Waste, VALSAT, Line Balancing, Blocplan
Subjects: Tehnik Industri
Divisions: Fakultas Sains dan Teknologi > Teknik Industri (S1)
Depositing User: Drs. Mochammad Tantowi, M.Si.
Date Deposited: 01 Sep 2021 18:40
Last Modified: 01 Sep 2021 18:40
URI: http://digilib.uin-suka.ac.id/id/eprint/43697

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